Jump to content

Johnny Mash

Regular Member
  • Posts

    16
  • Joined

  • Last visited

Posts posted by Johnny Mash

  1. The electric lumbar support motor in the drivers seat seems to have wound it out to a fully forward position and will not retract. :angry:

    When hitting the button to extend it further forward, it makes the typical noise and clunk of an outer thread unwinding and pushing against the very start of the inner thread where it 'hops down' after reaching the very tip of it. Attempting to wind it the other way (to pull it back in) results in maybe half a turn before it locks up, often accompanied by the overload tripping, meaning I'll be unable to use the motor for ~10 seconds. :blink: I've tried several times to get it to catch by just back and forward, but it never does. I've tried to be careful of them, but now believe that either the inner or outer threads - or both - could have been damaged and are now bent or stripped too fine to smoothly catch on again.

    Has anyone had this and been able to get the thread to catch again, or does anyone have experience in accessing the internals of the seat back and provide any information on how I could manually get in there to do it by hand?

  2. I'd re-seated the boot 2 days ago and it jumped out again today! :blink: Again - that sound Adamsy describes well - a wildly hissing Singer sewing machine at full tilt. The boot worked it's way out after some light 'feeling around' behind the brake with my foot, all before the replacement hose clamp job I planned for the weekend. The tube the steering shaft goes through is all rubber, and just poking around near there can deform the neck and thus pop the boot out. I've jammed it back in and bound it there with cloth tape for now.

  3. I don't know how it happened, and don't know if this steering shaft boot thing is mentioned much, but it seems so easy to dislodge. In the pics above, you can see where it eventually rode its way up and off the lower shaft and spun freely. If that's happened in the 2 months since I've had the car, perhaps it might be worth everyone giving it a look at one day.

  4. HI all,

    On Sunday I suddenly noticed some noise that seemed to come from behind the drivers footwell and its not nice :( . Its a very rattly clackety noise that is almost silent at idle, and obviously louder at high revs. Engine itself isnt running rough, oil seems fine, although may need a change soon anyway.

    I've heard the VVT noise online, and while I hope it could be that, I can't really decide what it may be.

    - Driven again tonight, sounds more like a truck in the vid than it actually does

    http://youtu.be/CAQ4TDBtJuk

    - no load, Park, revving

    http://youtu.be/3IJ_F1H6fEs

    I wasn't driving hard at the time or beforehand (as I was off to market, you see...lol), in fact I've been on a nanna mission and tried to economise to see how low the readout can get (9.0l/100 in busy suburbia is good)

    So guys ... I'd love to know what you think I'm looking at with this.

    SOLVED

    Hey guys,

    One overlooked issue is the steering intermediate shaft rubber boot. Its next to the brake pedal and sometimes easly kicked, so when its kick the boot can come loose from the housing for the boot.

    Obviously when this boot is opened engine revs can be heard from inside the cabin and sounds similar to what you were saying Johnny Mash

    I hope this helps!

    Regards Boondy

  5. my aurion sometimes cranks and doesn't start.... i found holding down the start button helped..... must crank the engine a little loner? lol i duno but it has been good lately. My battery was changed at 40,000km

    yeah sometimes i hold the key aswell to get it going but usually on the 2nd crank it gets going straight away

    Same FONGSTA, '07 with 67,000km... lol we both must have the SSG(EG) model as well! The "Starts Second Go, Every Go!" kind...

    Well, it actually will start on the first crank from a long rest in maybe 1 of 4 or 5 times. When it doesn't the first 4-6 sec crank frequently will just about make it, with a successful pop or two of life, then it will lose that kick and begin sounding like it's trying all over again, and cranking for it a few seconds after that doesn't increase success....

    But before that even happens, you've just gone for attempt No.2. coz it's easier. A third crank is never needed; the engine always catches on that second shot.

    my bet.. the one way valve in the pump is bleeding fuel pressure off over time, so when the car is cold / hasnt run for a while, the pump needs time to build rail pressure. to test this theory, turn the key on and leave on for 5 seconds before starting. Give sthe pump time to prime before engine firing. Does this make a difference? If so, its not a big deal, you can work around it, but may point to a fuel pump failure in the future..

    cruiseh, damn, could be that too. Cheers, I'll try that as well and take note.

    I have left the ignition ON at least twice on purpose to test your reasoning - and no doubt I've probably done it many times unintentionally as well but I don't remember how long it rested at those times - but all I can say is that it's not something I recall as being successful in the past. As we'd all agree, that sort of thing would let us fulfil our need to drive an Aurion for just that little extra longer! :toast: lol

    e: tone was wrong

  6. I did exactly this today and they're both quite simple mods to perform. The vac tube mod bypasses the electrical vac switch to now be 'always on'. Normally, this switch (and therefore the flap) is closed off at low speeds, preventing any vacuum reaching the actuator (the round part) that lifs this secondary inlet flap. Looping the tube back onto the switch is harmless. With the vac line directly on the actuator, it causes the flap to be open all the time, and you can test this at idle by removing the vacuum hose from the actuator and reconnecting it. You'll hear the flap opening.

    Lower resonator removal is very simple with a 10mm ratchet.

    Remove scoop bolt from above the radiator. Theres 3 vacuum hoses and maybe an electrical connector to disconnect, easy to remember - or label them. Disconnect - then + of battery, remove by loosening back nut enough to unhook the rod, remove battery & tray. Remove top intake duct, then the lower snorkel duct. The resonator will be exposed, and will come free after removing one bolt and finally levering out its plastic pushpin. Reverse to re-install, reconnect battery + then - . Your ECU will probably have reset. Mine did, and it idled high at startup for a minute, but normal from there on.

    I've covered over the gap in the snorkels resonator pipe with a tough foam rubber piece, shaped slightly larger than the hole, then duct taped and cable tied with a hard plastic backing on the foam to have it form a seal. The induction sound has come up to noticeable from feeling 'contained', previously but still nothing compared to having a pod filter.

  7. G'day,

    In with my 3rd Toyota ('83 MA61 Supra, '05 Camry Sportivo 3L V6), now an '07 Aurion Sportivo SX6.

    As much as I miss the manual in the Camry, the Aurion is quite impressive! Very stock now but looking to eventually apply some fixes, tweaks, and then pretty her up.

    Intake, exhaust, (uugh, that exhaust U-turn-then-Y-pipe weirdness),audio, ride, wheels and tyres, nothing OTT.

    Here to show my support for the information and experimentation provided by those who contribute their guides, fixes, and help.

    Happy driving!

    -JM

    e: I can't edit my profile - "[#1026] You are not permitted to modify all or some of your profile information.". Any tips?

×
×
  • Create New...

Forums


News


Membership